Don't rule out the manufacturer's troubleshooting recommendations!
I lowered the air to the tee in the attic to 20psi (it was set at 40psi) and left the flow jet psi at 40. Last winter I ran some
soap mixed with ethanol through this flow jet. I just ordered new flowjet part # FP57212 from KR
HCW,
Your setup resembles ours very much & based on this following "Honest to God" coincidence ....
This week we had the exact same issue... although it did not affect all of our 6 bays the same way. Being human we succumbed to not taking the time to calmly look carefully at the troubleshooting tips that
Flojet had on their service manual found at
https://www.kleen-ritecorp.com/files/88a54c5c-c317-48ad-acdd-d598d5e4d4db.pdf . Maybe we were just too overconfident, cynical & had one of those "know it all even though we didn't" moments ... I am not sure ... but I think we were feeling a bit embarrassed
& even scared ... especially since that glitzy looking brand new
credit card card no dollar
coins car wash located perilously close to us here in Bismarck is naturally looking to get as much of our business flow that we have worked so hard to build up over the years. We are trying very hard not to be jealous of their $$$ brand new ... less than a month old facility.
Long story short ... the following part has an o'ring on it: 20 - 3/8 STRAIGHT HOSE BARB (listed & shown on the above link). Upon close examination the o'ring looked "not as round" as it should have been. We had that specific spare part on hand. That solved the problem. Apparently, there was a slight leak at this liquid inlet port ... so the inlet for our liquid was not sealed good enough for the draw to occur properly.
So when you get your new
Flojet you may want to verify that the very inexpensive o'ring is not the culprit ... which will be OK because you really should have at least one spare
Flojet on hand anyway ... even though those pumps tend to be extremely trouble free.
Be sure & let us know what the final most practical solution is ... because I know that we all in our "hearts of hearts" want to be part of the solution & not part of the problem as pro business Ronald Reagon would reiterate many times much to the benefit of the American People ... despite those who made fun of him a bit too much
or worse yet had unjustified personal anger towards him.
BTW, we have always set our inlet air at 90 PSI which is within the 100 PSI
Flojet maximum spec ... for the simple reason if all six of our hogs hair bristle brushes are being used simultaneously ... the lathering foaming brush
soap will always be enough GPM on the liquid part of the mixture. To verify, refer back to the pump diagram (on the above link) showing the GPM relationship between the inlet air PSI & the potential GPM needed.
I apologize if this post is too windy & "heaven forbid" over the head of some of you reading it ... hopefully HPW ... the original poster will understand & appreciate it ... My intent is to be thorough & not to be too cryptic ... which some of us more experienced operators sometimes are guilty of. Like one of my college professors used to also say ... "The rest is obvious" ... a bit too much!!! He was not the best ... in my humble opinion ... especially when he was referring to the latest "everybody's doing it" 10 year trend etc.
mike walsh
http://www.kingkoin.com/USA_Deficit_Reduction.html